Sunday, November 30, 2025

Replacing some chips on 1130MRAM board based on testing

TOGGLING STORAGE READ AND OBSERVING THE SENSE OUTPUTS

I have the board set up with a switch that will drive a rising edge on the +Storage Read line, causing my board to emit a sense pulse for any data or parity bit whose value is a 1. The output has a pullup resistor to +3.3V and a sense pulse consists of a short pulse to ground for less than 100 nanoseconds, occurring roughly 800 ns after the rising edge of the triggering signal. 

SUSPICIOUS RESULTS

When the memory chip was not yet installed, most sense bits appeared to be a 1 and produced pulses, but not bits 2, 3, 4, 13 and 14. The two parity bits produced pulses when odd parity existed on the eight bits they covered - those were correct based on which bits were generating pulses. 

SEVERAL CHIPS COULD BE THE CAUSE

I removed the buffer chips to see if they were holding down the five erroneous bit positions. This is a tri-state buffer that will drive the data line on the memory chip when we are doing a write, but floats to let the memory chip produce an output during all other times. With the chip removed, all the data bits appeared to be a 0, thus it was the tristate outputs of the buffer chip that were sensed as a 1. 

The data outputs feed into a NAND gate which produces the sense pulse when the data bit is 1 and the timer chain drives the output pulse at the correct time in a read. One more chip is connected to the data lines, an XOR chip that is used to calculate the odd parity and produce the parity bit value. 

Thus, the cause for bits 2, 3, 4, 13 and 14 to act differently could have been the NAND gate, the XOR gate, the buffer chip or the memory chip. The memory chip driving an output during a read, the other three chips having a bad input that pulls down the data line. 

REMOVING VARIOUS CHIPS TO NARROW DOWN THE CAUSE

I desoldered various chips to help identify which chips needed replacement. With the memory chip uninstalled but the others there, I observed the problems. When I yanked the buffer chip from one location, the problem bits from that side seemed to go away. When I soldered down the memory chip but had the two buffer chips removed, the results were still mixed. 

There were some differences from the prior condition, but not all bits acting the same either 1 or 0. That could be the contents of data in the chip that are driving those results, but it could also be the XOR chip inputs causing the problem or the NAND outputs.

I had changed the NAND chip that produced bits 12, 13, 14 and 15, but still had the same results in the earlier tests before the memory chip was installed. However, I could have an issue with the chips that output 2, 3, and 4 - two different chips as one handles 0-3 and the other covers 4-7. 

ORDERING REPLACEMENT CHIPS

I have spare NAND chips on hand, but no spares for the buffer nor the XOR chips. I placed orders with Digikey so that I can swap in known good chips in these positions and continue my testing until I am satisfied that the sense outputs are working properly on the test bench. Only then will I move over to the 1130 and test with this cabled into the system. 

Tuesday, November 25, 2025

Finishing new PCB for 1130 MRAM, waiting on memory chip

CONNECTOR PINS INSTALLED AND MORE CHECKING ON THE PCB

I use square profile gold plated pins, soldered onto the PCB with the correct spacing, to form the SLT connector into which the three cables from the 1130 system will plug. A spare cable socket held under the PCB lets me orient the pins correctly as I insert them and solder them down. 

Everything but the memory chip is installed

I did more checking of the solder joints to the chips and connectivity of the key circuits. Using an external testing box I inserted a rising edge on the +Storage Read and +Storage Write pins, which allowed me to watch for the proper timer output pulses. They looked good.

Without the MRAM memory chip installed, the NAND gates that produce the sense bit outputs will see every bit of a memory word as a logic 1, thus each sense bit should produce an output pulse when I drive a rising edge on +Storage Read. Using the oscilloscope, I verified that this occurred as intended. I found a couple of anomalies to investigate. 

It also allowed me to verify that the parity generation circuitry would produce a parity bit value of 1 for both halves of the word, since each halfword had an even number of 1 bits (8) and the 1130 uses odd parity checking. 

WAITING FOR THE MRAM MEMORY CHIP FROM DIGIKEY

The shipment from Digikey is expected to arrive late Friday. I will be away visiting family (again) for a few days but by the end of the weekend I can get this soldered onto the new board. 

Sunday, November 23, 2025

Building new version of the PCB for 1130 MRAM

USING SOLDER PASTE AND HOT AIR GUN FOR ALL SOLDERING

Because so many of the chips are tiny footprints with very narrow pin spacing, I decided to use solder paste and the hot air station to solder them down. I mixed a bit of flux with the paste, which reduces some of the splatter after soldering. 

As the paste is turned into liquid solder, it forms balls. When the balls touch an exposed pad on the board, it flows onto the pad and other balls accrete to this structure. However, if a ball does not bump into a pad or other balls, it remains as a loose very small ball on the surface of the board. I had to clean these away otherwise they might move between pins to create intermittent shorts. 

I controlled the amount of splatter by applying the solder paste/flux mix carefully to reduce how much is away from the pads. I then dropped the chip into place with the pins aligned over the pad pattern. The hot air rework station as a control for the air volume, which I lowered because otherwise small parts like resistors could be blown out of place before the solder liquified. 

I used by PCBite with its small probes to test each pin for connectivity after a chip was soldered down. I touched up high on the pin with one probe and touched the far end of the trace with the other probe and listed for the beep of the continuity tester. I also touched adjacent pins to check for shorts. This was a slow process with all the chips and pins, but important to be certain that the board is correctly assembled. If a pin didn't have a good connection, I put on a dab of solder paste/flux and heated it until the connection was good while remaining free of shorts. 

First set of chips soldered down, circled in yellow

Another group of chips installed, circled in yellow

NEED TO ORDER A COUPLE OF CHIPS BEFORE FINISHING

I found that the main MRAM memory chip had developed a fault and one of the sense output NAND gates had developed a broken pin. I placed an order with Digikey and should have the parts before the week is out, when I can finish the board.

CONTINUING WITH NON CHIP COMPONENTS

I began to install all the resistors and capacitors onto the board. I used the solder paste and hot air station, even though these were easy enough to solder with an iron. In addition, there are a couple of connectors and all the pins that form the SLT connectors where the cables T1, T3 and T4 are attached. 

Tuesday, November 11, 2025

More work on retriggering issue with 1130MRAM

GOOD SUGGESTION FROM A BLOG READER

One of the blog readers, Merlin Skinner-Oakes, suggested that I add a low pass filter to the output signals that are causing the ground bounce. These are the eighteen sense bit outputs, open collector gates which pull the line to ground and sink around 8ma for every bit in the word or parity that has a value of 1. The more 1 bits in a word, the worst the retriggering. 

I had to choose a chip that could sink 8ma on every output, would be gated by the pulse from the second read timer chip, has an open collector (drain) output, and would operate properly at 3.3V. The selection was slim. The chip I chose has a very fast edge, compared to the SLT logic in the 1960s era IBM 1130 system. 

The initial values to test were 100 ohms and 100 pF, to see if slowing the fall time of the signals would lessen the problems. This establishes an RC time constant of 10 nanoseconds, thus the falling edge is spread over very approximately this time instead of falling very steeply. I can adjust these component values as necessary to fine tune if the initial results seem promising. 

BODGING THE CURRENT BOARD TO TEST THE FIX

The lines run directly from the surface mount output chips to the SLT connector cable pins. I will need to break the connection between the chip output pin and the cable connector pin in order to insert a resistor in line and a capacitor to ground. I would need to cut the traces on the top layer coming out of each chip, then run bodge wires from the relevant pins to my RC filter components.

This would be very messy to do with eighteen output pins and bodge wires to 36 discrete components. Instead I will test this with the minimum changes by altering only the two parity bit outputs and using a word of all zeroes. That will only produce pulses on the two parity bit lines, as these must have a 1 value to achieve odd parity. 

First two bodged RC filters on parity outputs

I just had to cut two top traces coming out of chip U11 to disconnect output pins 3 and 6 from the connections up to the connector cable pins. I then tacked on two wires at pins 3 and 6, connected them to an RC pair each, hooked the other end of the resistors to the T4 connector cable pins L9 and L10 and hooked the other end of the capacitors to ground. 


I had many frustrating setbacks with this work - it was extremely easy to form a solder bridge across the surface mount chip pins. When wicking the solder away, it was easy to break the link to the pad invisibly, so that a connection appeared good but was not. Solder could form shorts underneath the chip, not visible to the microscope. I even tacked a wire onto the wrong pin in one case. 

Each time I had to pull the board and do work at the soldering/rework station. Every manipulation threatens to break off tacked wires. I persevered until I had the board ready for its testing. 

TESTING RESULT

I had to store a word of all zeroes first, then perform a display of the word to see whether the spurious retriggering and ground bounce is suppressed by the RC filters I added to the outputs for the two parity bits P1 and P2. 

Initially I had more problems with solder joints as I worked on the chip to add the bodge wiring - one of the parity bits wasn't working due to such an issue. I finally got all signals connected properly with no shorts.

I was not seeing the parity check bits in the IBM 1130 being set by the sense pulses after they passed through the RC filter. The circuit that sets the flip flops depends on the falling edge of the signal to discharge energy in a capacitor. Previously with a prior output chip I found that the flip flop wasn't being set because the output chip couldn't sink the 8ma of current to cause the edge pulse in the 1130. 

In fact, the resistance of the RC filter lowered the current enough to either prevent the flipflop from setting or cause it to only set sometimes. I had to cut those out of the circuit to restore the setting action. 

GROUND ISSUES IN THE PCB ENTER THE CROSSHAIRS AGAIN

I did more measurements of the ground voltages on the PCB and found ringing of more than 500 millivolts up and down. They are coincident with the retriggering of the timers. If I can stomp this out, the rest should work properly. 

I removed the FET transistor to gain access to the big ground pad underneath, then soldered an 18 gauge stranded wire to it which is connected to the IBM 1130 ground bus on the other side. With this in place, the ringing was substantially lower, as you can see from the scope output below:

Yellow is the +Storage Read signal, purple is the P1 parity bit, blue is the P2 parity bit and green is the ground where I monitored it. The bounce was cut down more than 50% and the result is no retriggering. I am convinced that it is time to make an updated version of the PCB with special attention to ground to minimize the ringing/bouncing.